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Smartpour
on autopours
to
part 2
Introduction
Smartpour is a non-contact infrared temperature monitoring
system for molten metal streams. The detector is a ratio
or 2 colour device, powered from an electronics unit which
also enhances the noisy signal from the head and computes
a representative peak temperature for the pour. For long
pour periods, a temperature is computed every 20 seconds.
The system was developed to overcome a problem at Hepworth
Heating Ltd, Milford, Derbyshire on the company's Kunkel-Wagner
moulding line. Hepworth required more temperature information
between its melting furnaces and casting line. The company
already took regular dip temperatures but was unable to
increase the number of dips sufficiently, due to time limitations.
Separate infrared systems, on each of the four furnaces,
was too costly. A short trial on the pouring line proved
successful. Target distance variations of 5 to 10 metres
proved a challenge which was overcome largely by the skill
and patience of Hepworth staff in aligning the head with
the target. The first system was commissioned at Hepworth's
in November 1992.
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Automatic
pouring ladles
The first trial of a system on an autopour was encouraging
and appeared to be less demanding than dealing with asynchronous
moulding lines ie. manual pouring. Three infrared temperature
monitoring systems were successfully installed on autopour
ladles (pouring furnaces) during 1997.
1. Matsushita Refrigeration Industries (S) Pte Ltd, Singapore:
Matsushita are part of National Panasonic, Japan.
2. Potterton Myson Ltd, Warwick.
3. A major foundry group in the USA supplying the automotive
industry.
Matsushita Refrigeration Industries
The system, commissioned in February 1997, comprises a head,
in a totally enclosed water cooled jacket plus a smartprint
electronics unit . Range: 1100 to 2000oC. Threshold limit:
1250oC. The autopour is a Suzuka RGD pneumatic ladle which
feeds into a Disamatic moulding line. The head is installed
on the framework of the autopour ladle, viewing the pouring
stream at an angle to the Disa moulding line, from the rear
of the autopour, looking towards the moulding press. |
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Problems
dealt with
1. Transit damage assessment and rectification was the first
priority.
2. Various appendages on the ladle framework had been removed
since the site assessment survey some months previously,
the pillar earmarked for the detector head had been cut
off. It was decided, during consultation with their production
management, to site the head in a completely different place,
around the back of the ladle, away from the operator's working
area, this necessitated a substantial extension to the ladle
frame to provide a platform for the head.
3. Maximum ambient temperature specified for the head was
55oC. The actual ambient of the installed head was found
to be 70oC. A water cooling jacket was flown to site. The
head was fitted inside this jacket and an air line connected.
This did not give sufficient cooling so a water supply had
to be connected instead, giving the required temperature
drop. Air was still connected, to feed the air purge unit
on the front of the head. This minimised build-up of dirt
on the lens. Radiation from the autopour and the moulding
line plus conduction through the metal frame of the autopour
both contribute to the high ambient temperature at the rear
of the autopour. Matsushita's established routine for stream
temperature checks is to use a portable Disappearing Filament
Pyrometer (DFP) every hour. Temperature was measured with
+/- 10oC for each good pour. During commissioning of the
system a portable digital pyrometer with a short lightweight
dip arm and plug-in type 'R' thermocouples was used in the
metal stream to check the infrared temperatures obtained
and to tune the infrared, using the emissivity, E slope
potentiometer, at the rear of the head. The long reach element
of the thermocouple enabled minimal disturbance of the molten
stream. The limitations of accuracy of the DFP unit was
demonstrated and it was eventually agreed that the infrared
system to the existing DFP reading should be tuned. At a
meeting in November 1997, a problem with the infrared was
discussed. When using the 'inmould' system for nodular iron,
a recent development, one was unable to measure stream temperatures
into the mould, due to the flaring reaction. It was advised
that it was not possible to measure temperature with an
infrared system, under these conditions. The company was
advised to move its point of measurement back to the metal
stream into the tundish. The tundish is interposed between
the autopour and the moulding line.
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Problems
dealt with
1. During commissioning the autopour operator found the
apparently unstable reading on his indicator to be a distraction.
He was asked to ignore the readout until the commissioning
was finished. It was later explained that the program was
going through an updating procedure, as it searched for
a peak stable reading, which it finally held, until updated
by a new reading.
2. Shortly after installation, before handover, it was reported
that Potterton was obtaining apparent high readings. Burn-off
flame, hot gasses or metal dribble were suspected. Visual
observation dismissed the presence of any obtrusive target.
Metal dribble caused flashing on the temperature readouts,
but no final stable readings. Finally, for the record, photographs
of the metal stream were taken, of each stage of the pour,
including the push. The prints showed the presence of a
flame from the pouring aperture, only during the push. This
interference was eliminated by increasing the threshold
temperature limit to 1350oC. On the first trial of the autopour
it was decided to raise the threshold limit from 1200 to
1250oC to avoid interference from the burn-off flame, looking
down the moulding line, away from the moulding machine.
3. A requirement for this installation was downloading of
data to an existing computer for use with Lotus 123 spreadsheet
software for MS Windows. The first download program for
Potterton's computer matched its protocol requirements but
some data was lost. Finally, after an inappropriate delay,
a windows based program was supplied.
4. A variation in measured temperature with the infrared
system had been noted, when changing from one type of iron
to another type. To compensate for this change an adjustment
is need to the emissivity slope potentiometer, mounted at
the back of the head, near the eyepiece. Fortunately, this
potentiometer is linear, and a pre-set position can be established
for that iron type.
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